Loading…
Effect of temperature on the anaerobic digestion of palm oil mill effluent
Two continuous stirred tank reactors (CSTRs) each fed with palm oil mill effluent (POME), operated at 37°C and 55°C, respectively, were investigated for their performance under varies organic loading rates (OLRs). The 37°C reactor operated successfully at a maximum OLR of 12.25 g[COD]/L/day and a hy...
Saved in:
Published in: | Electronic Journal of Biotechnology 2007-07, Vol.10 (3) |
---|---|
Main Authors: | , |
Format: | Article |
Language: | English |
Subjects: | |
Citations: | Items that cite this one |
Online Access: | Get full text |
Tags: |
Add Tag
No Tags, Be the first to tag this record!
|
Summary: | Two continuous stirred tank reactors (CSTRs) each fed with palm oil
mill effluent (POME), operated at 37°C and 55°C,
respectively, were investigated for their performance under varies
organic loading rates (OLRs). The 37°C reactor operated
successfully at a maximum OLR of 12.25 g[COD]/L/day and a hydraulic
retention time (HRT) of 7 days. The 55°C reactor operated
successfully at the higher loading rate of 17.01 g[COD]/L/day and had a
HRT of 5 days. The 37°C reactor achieved a 71.10% reduction of
chemical oxygen demand (COD), a biogas production rate of 3.73 L of
gas/L[reactor]/day containing 71.04% methane, whereas the 55°C
reactor achieved a 70.32% reduction of COD, a biogas production rate of
4.66 L of gas/L[reactor]/day containing 69.53% methane. An OLR of 9.68
g[COD]/L/day, at a HRT of 7 days, was used to study the effects of
changing the temperature by 3°C increments. The reactor processes
were reasonably stable during the increase from 37°C to 43°C
and the decrease from 55°C to 43°C. When the temperature was
increased from 37°C to 46°C, the total volatile fatty acid
(TVFA) concentration and biogas production was 2,059 mg as acetic
acid/L and 1.49 L of gas/L[reactor]/day at day 56, respectively. When
the temperature was reduced from 55°C to 40°C, the TVFA
concentration and biogas production was 2,368 mg as acetic acid/L and
2.01 L of gas/L[reactor]/day at day 102, respectively. By first
reducing the OLR to 4.20 g[COD]/L/day then slowly increasing the OLR
back to 9.68 g[COD]/L/day, both reactors were restored to stable
conditions at 49°C and 37°C respectively. The initial
37°C reactor became fully acclimatized at 55°C with an
efficiency similar to that when operated at the initial 37°C
whereas the 55°C reactor also achieved stability at 37°C but
with a lower efficiency. |
---|---|
ISSN: | 0717-3458 0717-3458 |
DOI: | 10.2225/vol10-issue3-fulltext-7 |